Integrated Dry Nojso, Emissions Control System: Advanced Retractable Injection Lance Sncr Test Report

نویسنده

  • L. J. Muzio R. A. Smith
چکیده

The DOE sponsored integrated Dry NOJSO, Emissions Control System program (a Clean Coal Technology ill demonstration) is being conducted by Public Service Company of Colorado. The test site is Arapahoe Generating Station Unit 4, a 100 MWe down-fired utility boiler burning a low-sulfur western coal. The project goal is to demonstrate up to 70 percent reductions in NO, and SO, emission through the integration of: (1) down-fired low-NO, burners with overfire air; (2) Selective NonCatalytic Reduction (SNCR) for additional NO, removal; and (3) dry sorbent injection and duct humidification for SO, removal. The installation of the burners and overfire air system resulted in a decrease in furnace exit gas temperature of approximately 200°F. The temperature decrease reduced the effectiveness of the SNCR system at low loads. This report documents the third phase of SNCR tests (corresponding to the seventh test phase of the overall program), where an additional injection location was installed to increase the low-load NO, removal performance. The new injectors consist of a pair of retractable in-furnace lances which were designed to provide a high degree of load following flexibility through on-line adjustments of the injection angle. The majority of the test program was conducted using retractable lances proved by NOELL (ARIL lances). Subsequently, an alternative lance design provided by Diamond Power Specialty Company was evaluated. Before installation of the lances, the existing wail-injection location was capable of providing only 11 percent NO, removal at 60 MWe (at an NH, slip limit of 10 ppm). With the new lances, NO, removals in excess of 35 percent are achievable at the same load

برای دانلود متن کامل این مقاله و بیش از 32 میلیون مقاله دیگر ابتدا ثبت نام کنید

ثبت نام

اگر عضو سایت هستید لطفا وارد حساب کاربری خود شوید

منابع مشابه

Integrated Dry Nojso, Emissions Control System Baseline Sncr Test Report Subj: Integrated Dry Nox/s02 Emissions Control System Doe I.d. De-fc22-91pc90550

The DOE sponsored Integrated Dry NOJSO, Emissions Control System program, which is a Clean Coal Technology Ill demonstration, is being conducted by Public Service Company of Colorado. The test site is Arapahoe Generating Station Unit 4, which is a 100 MWe, down-fired utility boiler burning a low sulfur western coal. The project goal is to demonstrate 70 percent reductions in NO, and SO, emissio...

متن کامل

Integrated Dry Nojso, Emissions Control System Sodium-based Dry Sorbent Injection Test Report

The DOE sponsored Integrated Dry NO&O, Emissions Control System program, is a Clean Coal Technology Ill demonstration, being conducted by Public Service Company of Colorado. The test site is Arapahoe Generating Station Unit 4, a 100 MWe, down-fired utility boiler burning a low sulfur Western coal. The project goal is to demonstrate up to 70 percent reductions in NO, and SO, emissions through th...

متن کامل

Greenidge Multi-pollutant Control Project

The Greenidge Multi-Pollutant Control Project is being conducted at the 107-MW AES Greenidge Unit 4 as part of the U.S. Department of Energy’s (DOE) Power Plant Improvement Initiative (PPII) to demonstrate an innovative combination of technologies that is well-suited for reducing emissions from the nation’s large fleet (~60 GW) of smaller coal-fired units. The technologies, which include a NOxO...

متن کامل

NOx Control in coal combustion by combining biomass co-firing, oxygen enrichment and SNCR

There has been renewed interest in evaluating the effect of biomass co-firing on the multi-pollutant control system such as Selective Non-catalytic Reduction (SNCR) and oxygen enrichment. Emissions savings have been attained by combining SNCR and biomasscoal co-combustion under various oxygen enriched staged air levels. Biomasses with higher tendency of generating CO produced better reduction i...

متن کامل

Application of NO Reduction Dynamical Model in Selective Non-catalytic Reduction Denitration System Based on Biomass

In recent years, studies on denitration by applying biomass reburning method has drawn the attention of many researchers due to the characteristics of low sulfur and nitrogen content, high volatile, high ash focal activity, zero CO2 net emissions, etc. Based on Chemkin software and selective non-catalytic reduction (SNCR) denitration chemical kinetic model, this paper conducted SNCR denitration...

متن کامل

ذخیره در منابع من


  با ذخیره ی این منبع در منابع من، دسترسی به آن را برای استفاده های بعدی آسان تر کنید

برای دانلود متن کامل این مقاله و بیش از 32 میلیون مقاله دیگر ابتدا ثبت نام کنید

ثبت نام

اگر عضو سایت هستید لطفا وارد حساب کاربری خود شوید

عنوان ژورنال:

دوره   شماره 

صفحات  -

تاریخ انتشار 1996